First, as the investigation in either case is not complete, we don't know it was a malfunctioning probe. Second, if mx didn't know about MCAS like the pilots, they may not have associated the runaway trim with the AOA vane. In any case, the vane itself may not have been bad, certainly to look at it. Electronic signals and software are all down stream of the physical device.Wasn’t it a problem with the AOA probe? Surely they’d seen one of those before. That malfunctioning AOA probe caused MCAS to do what it was designed to do.
Also, if Lion Air mechanics didn’t understand how to fix the problem or have the parts necessary to fix it, then the mechanics should have said so and that plane shouldn’t have been flying again.
I believe the software fix isn’t to remove MCAS, it’s to limit how the degree to which it moves the pitch trim. The crews could have been alerted to the AOA disagree, but the airline elected to not have it installed.
“On 7 November, the NTSC confirmed that there had been problems with Flight 610's angle of attack (AoA) sensors. Thinking that it would fix the problem, the engineers in Bali then replaced one of the aircraft's AoA sensors, but the problem persisted on the penultimate flight, from Denpasar to Jakarta. Just minutes after takeoff, the aircraft abruptly dived. The crew of that flight, however, had managed to control the aircraft and decided to fly at a lower than normal altitude. They then managed to land the aircraft safely and recorded a twenty-degree difference between the readings of the left AoA sensor and the right sensor.”First, as the investigation in either case is not complete, we don't know it was a malfunctioning probe. Second, if mx didn't know about MCAS like the pilots, they may not have associated the runaway trim with the AOA vane. In any case, the vane itself may not have been bad, certainly to look at it. Electronic signals and software are all down stream of the physical device.
So you are saying because if you can overpower the UNCOMMANDED nose down trim with nose up trim from the yoke, it isn't runaway trim? I have reviewed my 737 QRH ( been off too long to recall it ) . I fail to see how one would not think Runaway Stab Trim was anything but the logical way to go in a MCAS abnormal. No other procedure comes close to applying.
I talked to one of our Mecs, he said there was no information about MCAS in any of their maintenance manuals.The lack of proper mx action makes one wonder if mx crews were as in the dark about MCAS as the pilots were.
Or like trying to fly with out altitude call outs on landings.. lol. Amazing how much I use that...Trying not to arm chair quarterback these specific incidents. We can't even be sure what kind of training they got. This is hangar flying.
We have had guys at my airline fly the entire return to landing with stick shaker from lift off to shut down back at the gate. They couldn't make it stop. They didn't know why it was happening. They just flew the plane. It was making power and climbing. Things like stick shaker can be very annoying and distracting. I get that. But remember, if VMC, as these poor souls were, does something like stick shaker convey accurate useful info to you when you can look out the window. Pitch/Power, anyone? You don't even need an AI if you are distrustful of instruments. You have a horizon.
For the yung'uns out there, don't ever let a plane do as it pleases (sez the guy who is bidding onto FiFi). Or as Bob Hoover said, "Fly the son of a bitch all the way into the crash."
It's a smart, thoughtful article, but the opener didn't exactly inspire me with confidence:Interesting perspective
One of the life experiences that comes with being a three decade veteran of military procurement
Everyone?Preliminary report shows the Pilots did follow Boeing's procedure but were still unable to recover.
This article discusses how, due to "excessive manual trim forces," it is possible for the 737 Max to be unrecoverable after disabling electric trim at normal airspeeds.
What a shame that everyone so quickly jumped to blaming the pilots because of the country and airline involved...
Preliminary report shows the Pilots did follow Boeing's procedure but were still unable to recover.
This article discusses how, due to "excessive manual trim forces," it is possible for the 737 Max to be unrecoverable after disabling electric trim at normal airspeeds.
What a shame that everyone so quickly jumped to blaming the pilots because of the country and airline involved...