THAT makes a helluva lot more sense than the other "knowledges" posts on the accident cause .... thanks.Without getting into too much detail, the reality of this accident is that the stud shut an engine down in the break (it was his first pass, not his second) and wound up in an adverse yaw departure when he tried to "come left" as per the LSO's correct call. ....
Side note: we had a crew that was left on the beach det @ CUBI as they were too weak to take aboard on that line period. As the LSO, I had suggested the pilot, fresh from the RAG, was not ready for prime time at the ship.
So they came into the break @ CUBI @ 500 KIAS, shut them BOTH down, didn't pop the RAT, and went "boom-boom" with the seats and the aircraft flew itself over to the beach north and opposite Grande Island. The pilot got his Wings pulled and became a priest.
The Skipper (a tool) hated me forever after for the blot on "his" record -- it wasn't his first -- like my recommendation had "caused" the accident. Small penises and fragile egos always amuse me ...